1966-073A
Lunar Orbiter I was launched at 1926 on 1966 Aug 10 by Atlas Agena D from Cape Kennedy. The Agena post-retro trajectory missed the moon by about 40000 km. On Aug 11 trouble struck when the Canopus sensor failed to acquire Canopus. The spacecraft attitude was calibrated by using the sensor to detect the Moon instead. Lunar Orbiter I made one mid course correction, at 0000 on Aug 12, and entered lunar orbit at around 1550 on 1966 Aug 14. The initial orbit was 191 x 1867 km x 12.2 deg. The periapsis was lowered on Aug 21 to 56 km, and on Aug 29 to 40 km. Lunar Orbiter I's mission was dedicated to surveying Apollo landing sites. The spacecraft was deorbited at 1225 on 1966 Oct 29 and impacted the surface an hour later.
| Lunar Orbiter I | |||
| Date | Time | Event | Orbit |
|---|---|---|---|
| 1966 Aug 10 | 1926:00 | Launch by Atlas Agena D on az. 99.9 deg | CK LC13 |
| 1928:08 | T+2:08 BECO | ||
| 1930:51 | T+4:51 SECO | ||
| 1931:12 | T+5:12 VECO | ||
| 1931:14 | T+5:14 Fairing sep | ||
| 1931:16 | T+5:16 Atlas 5801 sep | -4091 x 182 | |
| 1932:09 | T+6:09 Agena 6630 burn 1, 2:34 | ||
| 1934:43 | T+8:43 Agena MECO-1 | 88.3 189 x 202 x 29.6 | |
| 2002:34 | T+36:34 Agena burn 2, 1:28 | ||
| 2004:02 | T+38:02 Agena MECO | 194 x 348524 x 29.6 | |
| 2006:47s | T+40:47 Agena sep | ||
| T+49:43s LO solar panels deploy | 196 x 345551 x 29.6 | ||
| T+51:08 Agena retro | |||
| 1966 Aug 11 | 0214 | Canopus sensor failed | |
| 1966 Aug 12 | 0000 | TCM T+28h 32s 37.8m/s | |
| 1966 Aug 14 | 1532:33 | Begin LO burn 579s 790.0m/s | |
| 1966 Aug 14 | 1542:52 | LOI | 189 x 1867 x 12.15 |
| 1966 Aug 15 | Calibration film readout | ||
| 1966 Aug 18 | 1212 | Begin first photo sequence | |
| 1950 | Readout first photo sequence | ||
| 1966 Aug 21 | 205 x 1845 x 12.3 | ||
| 1966 Aug 21 | 0949:58 | OTM-1 Lower orbit 23s 40m/s | 56 x 1853 x 12.05 |
| 1966 Aug 25 | 1601:29 | OTM-2 Lower orbit 3s 5.4m/s | 40 x 1817 x 12.0 |
| 1966 Aug 29 | Photo coverage complete | ||
| 1966 Aug 30 | Readout of photos | ||
| 1966 Sep 11 | 30 x 1832 x 12.2 | ||
| 1966 Sep 14 | Readout of photos completed | ||
| Extended mission | |||
| Special tests | |||
| 1966 Sep 17 | Extended mission operations | ||
| 1966 Oct 6 | Stanford experiment | ||
| 1966 Oct 7 | Extended mission operations | ||
| 1966 Oct 15 | Commanding error, pitch commands | ||
| 1966 Oct 16 | V/H sensor tests | ||
| 1966 Oct 19 | Extended mission operations | ||
| 1966 Oct 27 | Special tests for mission 2 training | ||
| 1966 Oct 29 | 1225:49 | Deorbit burn 94s 0.1688 km/s, Oxid. depletion | |
| 1227:06 | At apolune | ||
| 1227:45 | Valves closed ater 115.7s, 6.4m/s | ||
| 1246:26 | depletion burn test, 2.7 m/s | -735 x 1831 x 12.2? | |
| 1249:26 | engine off | ||
| 1330 | Impact farside | ||
Payload:
- Cameras
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