1967-084A
Surveyor 5 was the first of an enhanced Surveyor type, the A-21A. It used the SLV-3C launch vehicle with a longer Atlas tank and higher thrust engines. It was launched at 0757:01 on 1967 Sep 8 by Atlas Centaur from Kennedy and rolled to an azimuth of 79.52 deg. The Centaur completed its second burn at 0816:27. A course correction was made on Sep 9 as planned, but a helium pressure valve failed to close properly after the firing. As a result, three extra course corrections were made to try and reseat the valve. Two more burns readjusted the velocity and aim point. A new retro profile had to be used, with a low retro burnout altitude of 1.4 km instead of 11 km. The retro was fired at 45 km altitude instead of 83 km, 12 sec later than usual. Landing was at 0046:42 on Sep 11 at 1.41N 23.18E (TR-32-1246).
| Surveyor 5 | |||
| Date | Time | Event | Orbit |
|---|---|---|---|
| 1967 Sep 8 | 0757:01 | Launch by AC-13 | CKAFS LC36B |
| 0759:34 | T+2:33 Atlas BECO | ||
| 0759:37 | T+2:36 Booster sep | ||
| 0800:19 | T+3:18 Panels sep | ||
| 0800:48 | T+3:47 Fairing | ||
| 0801:07 | T+4:06 Atlas SECO | ||
| 0801:10 | T+4:09 Atlas sep | ||
| 0801:19 | T+4:18 Centaur MES-1 | ||
| 0806:48 | T+9:47 Centaur MECO-1, 6:47 coast | 87.60 157 x 169 x 29.8 | |
| 0813:30 | T+16:29 Centaur MES-2 | ||
| 0815:25 | T+18:24 MECO-2 | 174 x 562308 x 29.8 | |
| 167 x 549654 x 29.84 (TMX-1844) | |||
| 0815:45 | SV legs deploy | ||
| 0816:27 | Centaur sep | ||
| 169 x 551802 x 29.83 (GD) | |||
| 0817:11 | Centaur lateral thrust | ||
| 0820:26 | Centaur retro | ||
| 0824:36 | Centaur blowdown end | 169 x 346337 x 29.87 (TMX-1844) | |
| 1967 Sep 9 | 0145:02 | TCM 14s 14m/s | |
| 0212:02 | TCM 10s | ||
| 0239:50 | TCM 23s | ||
| 0418:48 | TCM-4 12s, 13.8m/s | ||
| 0824:02 | TCM-5 33s, trim velocity | 1070 x 518304 x 29.2 | |
| 2331:00 | TCM-6 5s 5.3m/s | 773 x 520227 x 29.51 | |
| 1967 Sep 11 | 0043 | AMR on | |
| 0044:50 | Verniers on | ||
| 0044:51 | Radar sep | -770 x -11111 x 5.2 | |
| 0044:51 | Retro at 46km, 38.8s, 2.562km/s | ||
| 0045:30 | Retro off, at 1.26km 24.2m/s | -1737 x 1 x 5.2 | |
| 0045:39? | Retro sep | ||
| 0045:39 | Vernier high thrust | ||
| 0046:42 | Verniers off at 4m | ||
| 0046:43 | Landing | ||
| 1967 Sep 11 | 1237 | Centaur flyby 39850 km | |
| Centaur orbit | 167902 x 345368 | ||
| 1967 Sep 13 | 0538:15 | Vernier engine erosion firing expt. 0.6s | |
| 1967 Sep 18 | Oxidizer leak | ||
| 1967 Sep 29 | 0635 | Shut down for lunar night | |
| 1967 Oct 15 | 0807 | Activation for lunar day 2 | |
| 1967 Oct 18 | Solar eclipse | ||
| 1967 Nov 1 | 1220 | end of tx | |
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